Comments on the incident. |
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Red O'Laughlin - cleaning solvent drums were next to the ADI fluid and the wrong fluid was pumped into the aircraft. At takeoff, the water/ADI fluid injection was used. When the water was used up, the cleaning solvent, floating on top of the water, caused overtemps in all four engines and they lost power. The next plane ready for takeoff refused to takeoff and that plane also had the wrong fluid (cleaning solvent) in the water injection system. Good decision by the plane commander. |
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Bob Azbell - I was on a mission in Guam also and on our way back that day we found out about it on the way back to Cubi. I remember that day well as we decided not to use the water injection and it's a good that we did not as ours plus one other plane had been serviced with this dry cleaning solvent. |
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Red O'Laughlin - It's interesting in that the PPC got out of the plane OK, but broke his arm playing baseball (or something like that) a couple of weeks later. Many people thought he broke it in the crash. |
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Peter Clapham - John Werner was my SS-1 on Crew 4 and told me about this incident. Two things strike me about the story; the destroyer out in Subic Bay blasting Emergency and steaming right down on them and this ice chest breaking free of the aircraft as it sank, rushing to the surface with its positive buoyancy and hitting John in the chest from below while he was swimming. He got the wind knocked out of him and thought it was a shark. |
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Red O'Laughlin - If you notice the belly of the aircraft looks like it was opened with a can opener. The after action report said that the bomb-bay doors buckled inward and water hit the aft bomb-bay bulkhead and literally peeled the entire underside of the belly. The water came in and blew the aft bulkhead of the aircraft out. There was a passenger sitting in the galley and he literally got up and walked out the back end of the airplane. I inherited most of this crew a few months after this crash - learned a lot of inside information. |
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Red O'Laughlin - Another quick story, the SS1 who normally exits over the port wing was trying to open the window exit. The water was about half-way up the window and he had to wait until it was over the top of the window exit before he had enough power to pull the window inward. He then exited on the the port wing. |
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Charles Hudson - PC-6 was loaded with mines that morning to practice laying them. This was just before the US mined Haiphong harbor. The aircraft lost all hydraulic power early, and lost its pneumatic during the jetisoning of the mines in Subic Bay. Herbie hand pumped the bombay doors closed, getting back into his ditching station just before they hit the water. My memories are still clear about that day, but they are mostly second hand |
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Charles Hudson - Maybe it was the landing gear they had to handpump to raise. They appear to be down in the photos, but must have been up on impact. In addition to the regular crew, there were two photographers in the aft ditching station. On the first impact, the tail broke off right at their feet. To exit the aircraft, they unbuckled their seatbelt and fell out of the plane. |
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Paul Lusk Charles - I remember having to radio in to the Duty Office one afternoon when a car pulled off the side of the road up on the hill overlooking the AIMD ramp. The driver got out and was taking some of those "unauthorized pictures". I also remember having to extinguish a phosphorus fire inside the A/C while on watch. Truth be told...I'm sure it was the result of my walking through the aircraft. |
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Paul Lusk - I remember the AFT RADOME broke off and the entire contents of the AFT Radar compartment were gone, with the possible exception of the VOR racks. (The receivers were gone) I think Herbie jumped out the back as well. I remember reading a "Gramdpa Pettibone" article in "Naval Aviation News" a year or so after the incident. If memory serves me correctly, the Supply Department delivered the wrong fluid and the AK2 in 050, as well as the line crew, never caught the mistake. |
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Jim A Waits Paul - the phosphorus fire was caused by the smole-lights still in the storage box that were damaged and broke open during the ditching. I was surprised that no one ever called EOD to have those item removed. But, no one ever thought the P3 carried ordnance. |
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Robert Goggin - The 55 gallon drums of dry cleaning solvent were actually marked as alcohol drums and there was a navy wide message to check all drums. These drums had been cleared by supply as having been checked. Our squadron supply clerk certified they had been checked and I believe someone senior in the line also certified the drum had been checked. I flew in the night before from Cam Rahn bay and was the only rigger on base. They woke me up to inventory the flight gear of everyone on the aircraft. I believe there were 2 photographers in the galley seat and they are the ones that walked out the back of the aircraft. |
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Jim A Waits - The drum of cleaning solvent was on a pallet with four other drums of Methanol. The five drums were banded together with the solvent being in the center surrounded by the other four. Being banded together as a unit one could not view the markings on the side of the drums. Most important is how the drums were marked, Methanol and Cleaning Solvent were in Black drums with a White top. The accident investigation emphasisied that it was impossible to know the center drum was solvent instead of methanol. Another key element was the servicing cart that mixed and pumped the fluid into the aircraft was way out of calibration; there was no required calibration schedule required for it, hence as time went on it wasn't doing a proper mix. No one could have known the pallet of drums or the service cart could bring down an airplane. |
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